Ummduh
Red Skull Member
And straightened out the steering wheel, for probably the last time
Still ttb? Won't be the last time
And straightened out the steering wheel, for probably the last time
oh it will be, i just put it back together way off the last time. Wanted to make sure that it wasn't the cause of my blinker not blinking issue.Still ttb? Won't be the last time
oh it will be, i just put it back together way off the last time. Wanted to make sure that it wasn't the cause of my blinker not blinking issue.
It's not, it can do whatever it wants now
I just hammer a screwdriver into the body of the filter and use that to turn it. Makes a mess but is a great way to vent my frustrationGot that dang filter swapped finally. Had to remove the power steering pump and bracket to get in there with the 24" slip jaw pliers.
Had a small filter on there before, it was dumb.I just hammer a screwdriver into the body of the filter and use that to turn it. Makes a mess but is a great way to vent my frustration
68 Bronco - This is part of the stumble on light-load saga. Brief backstory, around 2200 RPM will start to stumble. Have gone through all ignition and fuel parts.
Latest thing I've been working on is rebuilding the Holley 4160. While I was at it I replaced the mechanical fuel pump with a Carter M6588, blew out the lines, replaced the fuel filters with quality ones (the clear plastic ones fell apart and were probably the root cause all along), and the aftermarket 23 gallon tank has a drain at the lowest point so I let a bit of fuel out of there (came out nice and clean).
Well, the last couple of days have been spent putting the carb on, start it up, sounds great, floods within a minute or so. Fuel comes right out of the primary vent.
Tried:
1. Smacking the bowl to free up a stuck needle/float.
2. Drained the bowl from the lower bolt, lowered the float and tried again.
3. Took the bowls off, swapped the float springs.
4. Checked that the floats float.
5. Took it apart and double-checked all of the gaskets.
6. Tried a different set of needles and seats.
7. Cleaned up the needles and seats real good.
8. Inspected the bowls.
Now I feel pretty damn comfortable tearing a Holley apart and putting it back together. I've watched multiple videos and verified my work. It still runs for a bit then floods out the primary vent.
Got pissed off an ordered a new carb that is on it's way... but I also bought a cheap fuel gauge and stuck it right after the pump before the carb filter. It runs like shit now and the gauge was at +12 PSI. I looked down the throat of the carb and there's fuel all over the throttle blades. From what I've seen it do the last two days it was probably going to flood out the vents if I kept it running long enough but it was running real rough.
Decided to buy a Holley 12-803 deadhead fuel pressure regulator. Going to throw that on and if it fixes it then I can return the new carb I bought. If it doesn't then I don't know what the fuck and I guess that new carburetor is going on.
With all that said, there are several forum posts out there talking about this specific mechanical fuel pump from Carter doing the same goddamn thing. Of course I only found this post today after my latest attempt to fix this goddamn thing: Carter (P/N M6588) Fuel Pump Warning
I've seen those be pretty far off, but what you are probably on the right track with the high fuel pressure.cheap fuel gaug
I know that pain all too well.New seatbelt, stupid T50 bolt.
I wrap a belt or strap around it 3+ times. You want to wrap it so as you pull the strap it is tightening around the previous wraps. Pull the outside strap while holding tension on the inside strap and the filter will spin off.Got that dang filter swapped finally. Had to remove the power steering pump and bracket to get in there with the 24" slip jaw pliers.
Has anyone said check the bushing in the distributor?67 Bronco: still on the stumble at 2200rpm under light load (like going up a hill)...
- It's not as bad as it was before the: carb rebuild, fuel filter fix, fuel pump + regulator
- I can now downshift and drive through the stumble
- I can do 70 on the freeway again
I'm still stumped as to why it occurs. Accelerating moderately up a hill will cause a less severe stumble/popping than it did before. Before it just refused to go past 50mph even if I downshifted. I can probably adjust the kickdown to shift even earlier to work around it for now.
My vacuum reading after tuning idle ended up at 18hg with a very tiny, rapid, vibration of the needle. I'm going to poke around again and see if I can find a vacuum leak but I've down a lot of that the past year and found nothing. Replaced hoses, tightened carb, replaced vacuum tree, new caps, etc.
Something I've noticed since I got this thing running is that it always had a faint smell that reminds me of a dead mouse/rat or nest/shit/piss when I come to a stop. It got me wondering if something is clogging up the exhaust, and wondering if that could cause a stumble like this. I've always felt since day 1 that this 302 should have a bit more balls than it does considering it has headers, 4 barrel, dual plane intake and was rebuilt in the last 5k miles (before I got it). It just feels like it's got a little lead in it's ass but once it gets going it's about what I expect. the 33's and 3.50 gears don't help but I've ran that exact setup before in a Bronco with a 302.
Just grab the rotor and wiggle it around.Has anyone said check the bushing in the distributor?
It would certainly do that. If the bushing is worn out the rotor starts hopping around in there when you hit the right rpms.
remind me, original duraspark distributor?67 Bronco: still on the stumble at 2200rpm under light load (like going up a hill)...
- It's not as bad as it was before the: carb rebuild, fuel filter fix, fuel pump + regulator
- I can now downshift and drive through the stumble
- I can do 70 on the freeway again
I'm still stumped as to why it occurs. Accelerating moderately up a hill will cause a less severe stumble/popping than it did before. Before it just refused to go past 50mph even if I downshifted. I can probably adjust the kickdown to shift even earlier to work around it for now.
My vacuum reading after tuning idle ended up at 18hg with a very tiny, rapid, vibration of the needle. I'm going to poke around again and see if I can find a vacuum leak but I've down a lot of that the past year and found nothing. Replaced hoses, tightened carb, replaced vacuum tree, new caps, etc.
Something I've noticed since I got this thing running is that it always had a faint smell that reminds me of a dead mouse/rat or nest/shit/piss when I come to a stop. It got me wondering if something is clogging up the exhaust, and wondering if that could cause a stumble like this. I've always felt since day 1 that this 302 should have a bit more balls than it does considering it has headers, 4 barrel, dual plane intake and was rebuilt in the last 5k miles (before I got it). It just feels like it's got a little lead in it's ass but once it gets going it's about what I expect. the 33's and 3.50 gears don't help but I've ran that exact setup before in a Bronco with a 302.
78 1-ton swap: now that the Bronco is out of the garage the woman might get off my back a bit and let me work on my shit. I need to rotate the axle track bar mount forward after I fixed the caster a few weekends ago. Once that's in place I think i'll finally start on the iBooster upgrade.
I used a 3/8" hardline between the tank and fuel pump. This is bigger than what is normally used, also probably a long shot.
Unless you have a leak on the suction side, the ⅜ fuel line is not your problem.some 5/16 fuel line
My bad, It didnt click that it was a 67' w/ points and duraspark wasnt until 74 or so.It had a Pertronix II in it. I replaced that with the whole Pertronix III distributor. Tested vacuum advance, checked timing, everything is good there. New plugs, new wires, new Pertronix III coil.
On the fuel side: rebuilt the carb twice, tank is a 23 gallon aftermarket I flushed that, replaced the fuel pump (that prompted me to install a pressure gauge and regulator because the new mechanical Carter pump was putting out way too much pressure) and that's running at 6 psi. Two new fuel filters (had an issue with crappy see-through ones which is fixed now), 100 micron after the tank, 30 micron after the fuel pump.
My two current theories are:
- mouse/rat nest in the exhaust/mufflers (long shot I know but it does have a faint smell once it warms up)
- I used a 3/8" hardline between the tank and fuel pump. This is bigger than what is normally used, also probably a long shot.
Drove it around quite a bit yesterday and while it was still warming up I got on a road going about 45mph and as it was accelerating it completely cut out like the fuel just shut off for a solid 2 seconds, then came back to life and was totally fine by the time I hit the stop light. There was no popping sound/backfire or anything like that.
I got a new Holley 4160 in a box from someone that I'm going to throw on there this weekend because I have it. Will give that a try just for shits and giggles (maybe I fucked up rebuilding the carb), and then I'll be ordering some 5/16 fuel line.
If that changes nothing then I guess I'll drop the exhaust and take a look.
Agreed, low HP like this isnt going to matterUnless you have a leak on the suction side, the ⅜ fuel line is not your problem.
I’d hurt my neck watching that thing drive by!Drug the '76 out and washed it. Been stuffed in the carport collecting dust the last few months.