Now onto the meat! I did that while waiting for the parts to show up from East Coast Gear Supply. I have never regeared or really messed with differentials at all, let alone one ton stuff so jumped in feet first. This always seemed complicated, but like most things after figuring it out and doing it it's actually pretty simple. I also had two friends (
RPS1030 being one) come over and help me over a weekend which was great! A lot of stuff was done, all the axle seals, the lock outs, ball joints, unit bearings, rear axle bearings, front axle shafts, axle seals, differentials, gears, I think the only thing that wasn't replaced was the rear axle shafts...
I went with 5.13 gears, this seemed like a good middle ground between 5.38s and 4.88s. I've seen some videos of people with similar drivetrain setups and 4.88s and they seemed to have plenty of torque plus the strength of 4.88s, but I was hesitant due to the 4l80e having a fairly high 1st gear and the Atlas only being 3:1 and since this will be more of a high speed crawler than a racecar that can crawl so 5.38s was appealing too. The rear is a straight up spool, my last racecar had a spool and I like the simplicity of them. The front is a Yukon Grizzly auto locker. The unit bearings are from Branik. The lock outs are from TMR. The RCVs are 35 spline. The rear shafts as I said are the stock 35 spline ones until I hurt one.
Fast forward about a week and finally got everything buttoned up and took it on it's first test drive! And within about 700ft the front end completely locked up. Luckily I had driven around the corner, turned around, and then it locked up so didn't make it very far from the shop. Pulled the lock outs so the front axles weren't engaged and drove it home.
The front rear pinion bearing had gotten utterly cooked, ate the cage, and seemed to have welded itself to the pinion.
There was no signs of lubrication whatsoever on the bearing. That combined with running the preload on the higher side is what did it in. The pinion angle is fairly high, I want to say like 17deg, and I had used the stock fill hole on the diff cover. Additionally, I hadn't installed the oil slinger for the pinion due to the OEM pinion not having one, so that bearing never saw a drop of oil. I tried a few different methods to remove it, beating the shit out of it with a sledge, tried melting it with the plasma, tried pressing it out with this contraption I welded around the axle...
Ultimately I dropped it off at a machine shop, though I first cut the steering skid off in the hopes a shop could fit it on their mill.
Which it ended up I didn't need to do, since the shop was able to use a torch to melt the pinion out! Might be time to buy an oxyacetylene setup myself... But for $40 I went from pricing out Spider 9s and thinking the housing was time for scrap to having it saved!
I called up East Coast Gear Supply and again hoping to buy just a pinion, which they said they couldn't do and it'd have to be an entire gear set which I kind of figured. So I bought another set of front gears, and they were able to get me just the pinion shims since I still had all the parts from the rebuild. I really have to thank ECGS, I had told the guy why I wanted just the pinion and then he had given me some advice which was awesome, and then dude said he'd give me a discount to help with stuff. I thought that was super cool, but I wasn't trying to save money, they had just been super helpful the first time so that's why I was going through them again. I figured dude was giving me like 5-10% off like most places have coupon codes for. When I got the invoice though the guy had given me a huge discount, and essentially made it so I only had to pay for the new pinion! I thought that was one of, if not the coolest thing a company has ever done. I couldn't care less if I had saved money and I'm just a random guy that was a moron and seized his diff on the first drive, and this guy at ECGS comes out swinging and doing everything possible to help me. I think that is extremely cool, dude had no need to do that and I would've recommended them regardless. So huge thanks to ECGS, you had earned my business from the first order, let alone the second order, and then to top it off with that is just so cool!
Anyways, I now got to weld the steering skid back on! So this poor thing is already seeing some scars and I don't think it's run into a rock yet!
I also bought some of the Spidertrax big fill plugs and welded that to the top of the housing so I can fill it as much as I want easily and have a view of the gears.
I only used the pinion from the new gear set. I couldn't find a definitive answer if the gears are matched to each other from the factory. I was able to get an acceptable pattern without touching the shims on the differential, which is why I didn't want to swap in the "new new" ring gear in case that threw the diff off. I figure worst case, it's an offroad vehicle, if there's some extra gear noise who cares. At this point I just want this axle behind me. I also opted to NOT install the pinion oil slinger and baffle, which afterwards I had some conversations and did some research since I was worried about that decision. In retrospect it wouldn't hurt to have installed those. But from my research it's a 50/50 call from people whether to install those. Some say for offroad they're not needed, some say for onroad they are needed, some say if they didn't come on the OEM don't use them (the advice I had followed). What I did do though is I installed everything and left the pinion seal OFF and ran the axles on the lift so I could make sure the rear bearing was getting lubed. I put in a LOT of gear oil, essentially the pinion gear is half submerged in oil, but what that means is the rear bearing is constantly in a gear oil bath.
Anyways, putting the front end back together. I also overfilled the rear by an extra couple quarts to be safe there, though there was no indication the rear was having issues.
And that wraps up last week! And then in the past few days I've done a few small things. First up was the front driveshaft is kind of a cluster, and ultimately was not able to droop enough without binding. So I pulled the yokes on the chassis side and machined them to clear more and now the driveshaft can fully droop without binding up. I'm not a fan of my driveshaft setup, I might revise it in the future but for now this will work. I also have a midship section (so small driveshaft off the Atlas to effectively a second mini driveshaft mounted on bearings in the chassis, which then goes to the actual front driveshaft to the axle) and I didn't know if I had remembered to lubricate that years ago when I installed it, so I drilled and tapped a fill hole into the midship housing (the housing that's welded into the chassis which then holds two angular contact bearings and then the shaft and two flanges), so the midship bearings are now actively lubricated in gear oil also. Though I actually had to pull the midship to machine the yoke, and found out I HAD lubricated the bearings with grease, so there's now a lovely grease/oil slurry for those two bearings!
I also threw the V-bands onto the header and exhaust instead of them being tacked together. I also bought some additional O2 sensor bungs so moved the wideband sensor to a better spot that wasn't poking through the floor.
And that all leads to yesterday where I went on the first successful 4WD drive! And I was extremely cautious about measuring the temperature of the housings at the pinion bearings to make sure I wasn't cooking them and so far everything was behaving as expected!
This thing is god awfully slow still. It was horribly slow before, and it's still so slow I don't even notice/remember a difference from the 3.73 gears it had. It might be time to build the 408 stroker motor sooner rather than later... but it runs and drives again! Plus a bunch of other little upgrades! Maybe take it to Sand Hollow this weekend and finally get it in the rocks. The next thing I want to do is build a proper fan shroud for the two radiator fans, I think that will be the next project.