Ended up getting talking into leaving Thursday night at 8pm....
Got to Bakersfield around 2:30am and tucked in my copilot
Woke up at 5:45 and ran the rest of the way down, but not before checking the scales at the truck stop we slept at. Extra thiccc

. Pulled the pass at 62mph and the exhaust brake had plenty of balls to slow her down, tapped the brake a few times and i have zero concern that she'd pull down in a hurry if the EB ever failed. She pulled 70-72mph on the straights and averaged 8mpg round trip per the liometer.
Of course had to go to backdoor the first night, 3 hours of sleep and a 22 hour day the day prior. Seemed like the best idea i had in awhile. Cutting the stinger off made the approach way better
Unfortunately that hole was DEEP this year from the rain/snow and that big ole booty judy departure angle just wasn't going to be overcome with tire spinning. Completely unloaded the rear suspension and just sat her ass in the hole like the stubborn bitch she is. Didn't stop me from letting the BB sing a little though
Slept in the next day and then went out to the suspension tuning area. Phil at liberty mountain fab really is Shock Jesus. No videos because i smashed the go pro at chocolate thunder but she was eating whoops at 65-70mph. ear to ear grins the whole time.
Overall it was a great trip and good times with some good people i hadnt had a chance to sit around a smudge pot with in a long time. But it was not without its share of carnage
Damage List:
Lost a rear spacer and ejecto-seato the wheel assembly into the mud pit of the lake bed, that sucked. Looked like 6 of the nuts on the spacers came loose because those 6 studs looked great. Sheered two of them. Farm jack in the mud and man handling a packed full 43 was a good time.
Trans did great, checked fluid twice and it was fine, i have a suspect for the leak though
Body damage from back door, lost a tail light, tailgate has seen better days
Starter loosened up back by the dunes, by a stroked of the KOH gods i found the stud in the dirt, threaded it back in, tightened the starter and now its overshooting the flywheel...never done that before... SO i loosened it back up, held it off the mount with a wrench and it grabbed great. So short term solution would be a starter shim
BUT
I think the spacer depth is wrong on the 8 bolt pattern for my 8hp75 trans. The adapter i modeled after is for a 8hp70/90, which in theory should be the same but the depth is obviously something is off. To compound on this i think the leak is the seal on the TC being pulled to far towards the engine. IT would align with leak condition being only on higher RPM and would align with the start spacing being off. So i think yanking that trans back out is in my future