What's new

1980 F350 Farm Truck Re-Build

alright, this is from the 1985 wiring diagram. Not shown on the next page is where the single wire lead #16 R-LG runs to the + side of the coil. sooo....if I can find a splice 216 or a BR-PK wire up near the firewall, I can check there for 12v+. Since i'm not using a throttle actuator, if I can't find power there, then i'll just borrow power from the starter solenoid for the coil.

splice.png



a couple key differences on the 1985, there is NOT a clutch safety switch on the 1980 as well as no EEC for emissions, the 80 is lots more temp switches and vacuum lines it seems.
 
alright, proof of spark during cranking. had to get the wife to help out so that I could see and hold key to START.



Pocked and prodded with the multimeter with the starter unhooked at first, everything seems to be doing stuff. Went ahead and filled up the fuel bowl and squirted some fuel down into the intake. Had the wife help again by standing up front to see if the pump was pumping into the filter and if things were doing stuff. Took just a little bit of fiddling with the choke and it actually popped off okay



Fuel was bubbling out of the fuel float level adjustment. adjusting seemed to be moving, decided to pop the bowl half off and see if something was stuck or what all was going on. This was running reasonably poorly due to a host of issues and then sat on the shelf for a couple years.

4 bolts that were less than hand tight and the fuel inlet and it popped apart with gentle taps

20240217_165238.jpg


It was always a slim chance that this gasket would survive, it decided to mostly tear in half.

20240217_165232.jpg


Overall the bowl was pretty clean and the accelerator pump works and pumps, so that's neat. This is after spraying it down and wiping it out.

20240217_165509.jpg


and the inside view looks pretty decent

20240217_165452.jpg


photo evidence it's got # 73 main jet currently. Did pick up weld in O2 bung for the exhaust, going to see about getting that cut this weekend or so to do some wideband tuning

20240217_165813.jpg


turns out the needle and seat come out the top and there is no reason to pop the bowl off :laughing: cleaned it up and verified it is operating smooth and easy

20240217_170027.jpg


plugged it all back together and got it started one more time, ran briefly until the bowl was out of fuel again. Wife's theory is that the fuel line between the filter and the carb is too severely kinked. She's probably correct. Should be much warmer than 30* tomorrow, going to make a new line then and try again.

picked up some clamps to make quick and dirty exhaust hangers as well, then it will be time to see if i can dial in tuning, get fuel into the tanks and see what happens. Might work on some of the accessory wiring
 
Fuel lines was the goal for today, beings the tanks are now out and ready to go back in once the sending unit lock rings show up.
....

wanted to put the cheap replaceable filter somewhere that was both easy to see and easy to replace. Between the holley and the distributor seemed like the thing. Had to make a bit of a wonky bend to resolve the angles, you can see the crimp that went too tight when manipulating by hand near the filter :laughing:
20240101_144358 circled.jpg


Found it, might have been funny on January first, but whose laughing now? :rasta:



me again, i'm also laughing about it now :laughing:
 
I'm pretty sure that I pointed out that kink as a problem at the time:shaking::laughing:
There's some key elements I'm not going to be real surprised if they turn into issues.

Wife goes "it kind of sounds funny" well yeah, never did fix all the exhaust studs and the exhaust is still just mostly together. That buys me some time for noise :laughing:
 
I've packed fine sand in lines to help bend them without kinking.
I've tried that a couple times with various sizes and never had much success compared to the hassle. This one was a "eh, just need a little more" so I hand grabbed it and it gave, opened it back up and it came back some.

Current theory is some is not enough, not really anything else in there for it
 
Still a little cold this morning, should warm up once the sun gets overhead. guess this filter needed replaced anyways, had about 30 second of use

20240218_093655.jpg


made the loop bigger and am still up off the valve cover

20240218_100801.jpg


this is all i've got left from my roll of 5/16". wasn't enough to go around to the back and put the loop behind the carb.

20240218_100828.jpg


and all that to have no real change. looked for my timing light, can't find it. not sure if it died or got lost in the move and I can't remember where I saw it last. looked at the carb and this screw is real far back from whatever it lands on, spring is not set to spring anything, might need some hokey-ing with. might just need to be bottle fed for a little bit yet to stay running before it will want to idle

20240218_102040.jpg
 
Indeed it does, they move together as well. the whatever it lands on comment was more a note that i'm not real sure what it actually actuates or why it does anything. moving the choke still moves up the throttle for choke high idle and the curb idle is adjusted much lower.

Holley seems to think the landing pad needs to come up, which means i think i'm going to go pop it off the manifold and see what there is to see. if nothing else, it's in the wrong position

0-4412c.jpg
 
20240218_132228.jpg



Couldn't find the timing light or my analog voltmetet/tach, twisted dist until it was close enough. Best I could get from twisting the knobs on the carb was 18-18.5 inches and 600 rpm idle.

Eventually it will be worth investigating the dash issues, until then it's a decent runner. Wire the exhaust put of the way so I can m9ve it in the yard and finish that up
 
alright, let's see what other pictures i've got

Got the carburetor popped off, this thing does nothing and isn't linked to anything. it can stay floppy, other option would be to remove it, but that seems excessive

20240218_112302.jpg


kind of neat while looking over the thing, the idle screw wasn't actually touching anything. kind of hard to tell in this picture, but there was some gap there when fully off the choke

20240218_112341.jpg

Played around and reset that so that it would expose the long slot idle bleeds but not the mains just above the throttle blades. Also pulled out the idle mix screws and foamed some goo through those as well

20240218_112920.jpg


plopped it back on, used the autogage tach, just kind of twisted the wires and stuffed them into places. Not sure why the dash tach isn't working today, other than a couple of pulses, it didn't register at all. Video a couple posts up in #253, but it is running smooth and idling well. didn't take much twisting beyond the 1-1/2 turns from bottomed for the idle screws. 600 rpm is what the valve cover asked for, 18" of vacuum is what I could get up there. I also went ahead and got fresh gas and dumped it into the rear tank, for some magic reason the tank selector solenoid didn't want to stay energized to pull from the front tank :laughing:

20240218_131556.jpg


here is a better picture of the crease I hammered into my straight length. The more I look at it the more i'm tempted to replace it with a real bent piece and getting into a better spot. just a little bit bummed I missed that angle by so much when I did the 2 into 1

20240218_151643.jpg

Finally cut and hammered this thing off and cleaned up the rest of the factory mounts off the scrap pipe

20240218_151648.jpg


and used some 5/16" rod with a couple bent ends to make a hood prop, now I don't have to grab a piece of pipe all the time and it staying in whatever clamp was already there

20240218_160156.jpg


Here is where it sits, once that is together it'll be a cruiser.

20240218_154232.jpg


front bumper back on, something for the rear bumper and hitch receiver, and figuring out why the radio, dash and all sorts of electrical things don't work.

At this point it feels like a bunch of the major stuff is done though, so that's nice.


proof it goes forward, stopped to make sure it went backwards before pulling into the road to get turned around

 
2-5/16 trailer ball is super handy for reforming 2-1/2" exhaust

20240219_110626.jpg


and here is the kinked section, i ended up using a couple of 45* to clear the trans crossmember and needed some straight. Put me right about where i'd creased it previously. What it started with on top, what I ended with after hammer, pliers, trailer ball on the bottom and a reference "good" section on the left

20240219_110855.jpg


7 slices was the appropriate number to make the gentle bend and right all my wrong angles

20240219_115955.jpg


gave it the old cut where it touches and you don't want it to

20240219_140609.jpg


and weld where it does touch and you want it to stay. the factory mount remnants off the junk yard tube made contact with the retrofit hanger, pretty sweet

20240219_140636.jpg


and added a hanger to this clamp. I don't really know why I went at such an angle, but it made sense at the time when i was under there

20240219_140559.jpg


Just a hint of evidence that my quick shitty welds the other day aren't exactly air tight :laughing: not really worried about it on this thing, might slap some spray paint on there, but i'm figuring it'll last long enough for what I'm doing to be not a big deal.

20240219_140546.jpg


and it looks like it belongs

20240219_141529.jpg


If i can come up with a spot to add another hanger i will, but for now the 2 seem to be working fine

20240219_141535.jpg
 
I was really hoping for a very quiet stock sort of sound, maybe if i'd used a new muffler instead of a used one. As it is, other than the sound of a couple exhaust leaks and the manifold leak, it sounds too open. However, it cannot be beat for the cost and it gets the vast majority of the fumes behind the rear axle, so all in all, complete success. Drove it around the block a few times to make some loaded pulls. Steering/toe still isn't set, brakes work and it shifts like it should.

Speedometer works, that's a plus :smokin:

20240219_144852.jpg


Real slight fuel leak from this fitting, i'm going to have to try out my old flare set instead of the newer one

20240219_142403.jpg


also looks like a really small leak here.

20240219_142410.jpg


power steering feed line was very loose, but that stopped leaking after tightening it down. Hosed it off to see if the leaks are done leaking.
 
Add a glasspack in front of the muffler.

Impressed you pushed thru and got this thing on the road
 
Add a glasspack in front of the muffler.

Impressed you pushed thru and got this thing on the road
Thanks! Glasspack would help a bunch, probably even one of those resonator tips would be enough to quiet it down. It's not too bad overall. Certainly could be worse and it's better than the other day when it was pretty well just straight pipe.

I'm happy I ended up pretty close to my original $3k price guess, sure did go way longer on time than I figured
 
What is the first job for truck?
Build a garage for itself

 
Is that a 30 spline dana 60 rear? I dont have much experience with the pre sterling 10.25 85ish 3/4 & 1 ton bullnose trucks
 
Got the carburetor popped off, this thing does nothing and isn't linked to anything. it can stay floppy, other option would be to remove it, but that seems excessive

20240218_112302.jpg
That floppy lever would be for an auto trans kickdown lever.
By the way, just read the whole thread. Good job keeping with it and getting old iron on the road again!
 
An old trick when using paper holley gaskets, is coat them with chapstick and you will usually get to reuse them.

Thanks, these came like that amd split I'm half. Conveniently, they still hold fuel. I did pick up the blue reusable gaskets and those will live in their packaging in the glove box for the inevitable next time it comes apart. I am still on the likely side for getting the oxygen sensor hooked up for some more tuning and such

That floppy lever would be for an auto trans kickdown lever.
By the way, just read the whole thread. Good job keeping with it and getting old iron on the road again!
Thanks :smokin:
 
I'm probably up to a post for this thread

Here is the old inner tie rod for the drivers side, gentle pressure on the front/back of the tire and it flops side to side, despite being freshly greased. New tie rod end holds up much better.




This also took care of the excess camber I had going on with that side. Set the front end on jack stands and took the drag link off at the steering box. Recentered the steering wheel, 2-1/8 turns from locked, and played around until the wheel was about centered, the tires looked mostly straight and the toe was about 1 to 2 eighths of an inch inward

20240310_123258.jpg


20240310_123323.jpg


Set it on the ground and it looks to be significantly improved from where it was before. Yay!

Since I was already on the ground, wiped off the crank a bunch and gave it a shot of paint to see if it would be easier to read

20240310_124427.jpg


Better than the miserable that it was before, still not legible under the light. kinda-sorta can see it :laughing: pretty well sticking with the 10* as recommended by the sticker.

20240310_124749.jpg


popped open the hood....stupid old plastic, being all brittle and stuff

20240310_124840.jpg


new 3/8" return line for the power steering pump

20240310_130330.jpg


and my puller decided today was the end of it's life. Last time i used it, had to use vice grips and pipe wrenches to keep it together. Borrowed the Loaner kit from the parts store, went much faster :laughing:

20240310_164629.jpg


and a bad picture that i'm not sure why i took, but there it is :rasta:

20240310_170318.jpg


and beings this was the absolute worst master cylinder i'd ever seen, and I tried to just use some sand paper and a finger instead of a hone to "rebuild it", I ended up going with a full replacement unit. This one doesn't seem to leak out of the fittings or the rear, which is pretty neat

20240310_152912.jpg


and crossover from the useless things about your ford from the other weekend, got my hitch receiver installed. Didn't get around to making a rear bumper or a brace for the receiver today.

20240303_162724.jpg
 
Top Back Refresh