4 days later after I tied up a few loose ends I gave the truck another try. Made it around the block. Engine was a little better but still had an incredible exhaust tick. Still fighting the fans but I wanted to get some miles on this thing so I setup a couple bypass circuits.
Logged 48 miles that day. Not all bad but lots of issues. No weight in the rear makes it very loose. Was fighting water temps.
Steering/front geometry is fantastic. I was overdriving the truck a little more than I should have. Had to remind myself it’s not the ultra4. The steering gear is a temporary Frankenstein using many parts I had leftover stuffed inside the casting from the ultra4. It wanders like hell. There’s a fix coming up soon for that.
Transmission seemed fine but once it was hot it did not like shifting to 3rd. Engine oil pressure was pretty good throughout but even with my mods and new bearings etc, it still only has 15psi hot idle.
I need to run a test without shocks to determine if the poor ride is from the springs or $50 no name shocks. The rear suspension shifts terribly during cornering. I need to see if there’s some leaf spring tech to hold the pack together or I need to install a panhard
Parked so I could replace the header gaskets and some other loose ends. Doing some reading I discovered why the transmission didn’t like to find 3rd. The modulator pin was missing. Previous owner had removed the modulator and I wasn’t aware of such a pin. So I borrowed one from a donor. Now 1-2 and 2-3 are much more consistent. R code servo is the next mod
Removed pass shock tower to relocate for more header clearance
Rear pinion yoke leaked like a mofo even with new seal. Pressed a speedi sleeve on and no issue since.
For the headers I used Patriot dead soft aluminum and while not the issue, some stage 8 bolts. I used my clutch fan bar to torqued these bad boys. In hindsight that was very unnecessary.
Found another vacuum leak. I never tightened the pcv connection on the valve cover. Now I had a pretty steady needle and increase from 14 to 18hg. Not without a bunch of drama. I discovered the Pertronix rotor was installed 180* out. Luckily the rotor wasn’t damaged but now I had to time the engine again. Well I didn’t include photos but I converted this centrifugal dizzy to vacuum advance. It had to come out anyways. When it came time to fire up I had a bunch of trouble. It refused to start. Acted 180* out. Lots of fits. When it would fire it had no throttle response. So I walked away. Came back another day and started from scratch. TDC yada yada yada. It started but wasn’t happy. Among some Pertronix issues I think the other side was collapsed lifters and some semi fouled plugs. All good now.
On the next drive my front calipers were locked up. Smoked em good. Learned a cool lesson in my MC thread about swept volume and identifying port locations. Turns out late model stuff is opposite of old school MC’s. Well that sorted out some issues. The calipers aren’t locked but now the drums drag. That goofy fitting seen on the rear is a residual pressure valve. My issue was F/R lines were backwards.
Tinkered with shimming the core support to dial in the door gap. Much happier now.