3.4 was sipping coolant to the point of hydro locking when sitting for too long. Yanked it out and put in the $100 "ran when pulled" motor in. Threw a minimal amount of parts at it: plugs, valve cover gaskets, and moved my intake/motormounts/exhaust/ps/alt over to the new motor.
Bringing the "new" motor up from the shed to the garage.
old abused "mud truck motor" coming out.
The most pita part was the newer motor was from a 2000+ 4runner with the forward dipstick. Drilling the hole took forever. Used a cobalt bit with kerosene for lube (google said that the combo to use)
I did the 3.4 "swap" October of 22, so this was just a regular motor swap. I was unmotivated and busy with the wife so I took my time, about a month to get it swapped in.
It looks the same as the old one because I reused my painted intake and valve covers. Got it completed Sunday and took it into the woods Monday after work..
And proceeded to flop it as we were headed out of the woods for the evening.
Got it right side up it and let it sit for a a few, fired right up and drove out.
Back to wheelin now!