It's been a crazy busy few weeks, I'll go ahead & document that here for those interested, For those that are not, the last couple lines of this post will get you up to speed on this build,
When I last posted I was ready for test drives & tuning on the new engine, well the first couple test drives went great! The new engine ran so good,
I'm just going to copy & paste my FB recount of the events leading up to the Havoc event this year.
"After several years of joking around about how little maintenance I have to perform before the big show, karma finally started joking back with a couple major failures in 2021 & 2022,
This year I planned the long overdue new engine, & better accessory drive, to go along with the new transfer case that was installed the end of last year,
Unfortunately after many long hours I was still going be kicked right in the guts.
Engine assembly & installation, while time consuming, went well,
Same with all the fab work involved in the new belt drive system, & completely new steering pump system, followed by the new fuel cell,
The new engine ran awesome, & even before fine tuning was looking to exceed our expectations,
While confirming ignition timing (Not even 10 minutes into the first tuning session) the new engine developed a pretty bad noise,
I shut it down immediately & began investigating,
Turns out a brand new Comp roller lifter come apart, ruining any chance of this engine running this year.
This was basically the last set of days off to actually work on the rig & have it ready to go.
After talking with my “engine consultant”
We decided a visual inspection & new bearings in the ole 513 before re-installing it would be the best chance of me still making it to Havoc.
An early trip to Reno the next day I was able to get a set of bearings & gaskets from summit racing, & be back to the shop before noon, plenty of time to roll bearings in before calling it a day, right?
Maybe, if I didn’t notice the crank shaft was able to turn about 45° back & forth without the camshaft moving,
Closer inspection there found a broken cam dowel pin,
Thankful that catastrophe didn’t fully play out, I removed the upper timing gear, & all 3 pieces of the dowel, set the gear up in the mill & drilled a second hole 180° from the original, followed by doing the same to the camshaft,
After installing TWO new dowel pins & a better retaining washer, I was feeling pretty good about the repair & looking forward to finally getting those new bearings installed,
However, in the famous words of Billy Mays, “but wait, there’s more!”
While doing a final inspection of my work at the front of the engine, something caught my eye, & sure enough, this engine too had a damaged lifter, not to the point of the new engine, but it was well on its way,
(Right about this point is probably the 4th time I said “I’m done”)
Oddly enough, my normally pessimistic yet great friend & "engine consultant" popped off with “well you do have that set of lifters you saved out of your car”
So I continued on
Running out of days (and parts) my second to last day off included putting in new/used lifters, reinstalling pushrods, rockers, girdles, & setting the over head,
Then finally installing those damn bearings, & sealing it up with an intake, oil pan, & rocker covers,
Finishing the day with a personal best of 2 hours to remove the engine out of the buggy, & remove the remaining parts I would need off of it.
My last day off, got the engine installed & the buggy back to a runable state,
After a week at work, this weekend was supposed to be for getting loaded & ready for the trip, but I still needed a tune for the buggy, & long story short, uploading the old tune just wasn’t an option,
Fortunately, Josh West worked his magic,
And in less time it took me to wreck the last engine, he had this one dialed right back in,
I also have to thank my wife for getting a few things done that I simply wouldn’t have got to.
So here we are, one more full day to make sure everything is good, & get loaded,
I’m not sure what I’m bringing this year,,,but I’m bringing what I got."
The following weekend we made the long trip to Bonners Ferry ID for the 3 day event, the buggy ran flawlessly, & even though I made a couple petty mistakes, my co-driver & I were able to land a solid 4th place finish overall out of 21 solid rigs & competitors,
The two most difficult courses were where we performed the strongest, so I was real happy with that,
(Here's a pretty good video of our rock course run)
So, Where I'm sitting now, I'm certain the engine guy is going to want to tear the 528 down & get going on that, however, right now I'm really considering putting all the buggy/event stuff on the back burner & focus on the project this thread is about,
I feel this project needs to get done,
I do have a new tool that I purchased a few weeks ago that I need to get setup (more on that in upcoming posts) hopefully that will be up and running next weekend, make a few small repairs to the buggy, then back to full steam on the Midnight panic project.